iamtherealJayy
Full Access Member
- Joined
- Nov 26, 2021
- Posts
- 1,584
- Reaction score
- 277
- Location
- Tennessee
- First Name
- Jacob
- Truck Year
- 1987, 1978, 1976
- Truck Model
- V20, K10, K10
- Engine Size
- 350, 350, 350
So I finally got around to showing my original truck some love, and as always it has fought me every step of the way. I got the throttle body out cleaned up all new gaskets etc. I took the tps and iac out to clean it. Got everything back on and assembled, truck fired instantly and idle I let it warm up to reset the iac, shut teuck off jumped a and b on aldl ignition on wait ten seconds unplug iac turn ign off and remove jumper. This is around where the issue started, I had to give it some throttle to get it to start after this. I got the tps set at .58V at closed throttle. I can rev the engine from the throttle linkage and it returns to idle, I can then press it closed a little bit more and it will stall the engine. It also cranks for around 12 seconds now.
Videos-
Did I somehow reset the iac completely wrong? It just doesn’t make sense how cleaning it and resealing all the leaky parts made it so much worse.
Videos-
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https://youtube.com/shorts/GhZpcS55pQs?feature=shareDid I somehow reset the iac completely wrong? It just doesn’t make sense how cleaning it and resealing all the leaky parts made it so much worse.