Strange wiring issue, killing ignition module

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highdesertrange

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kalifornia
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mike
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1978
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k30
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454
first off 1972 did not have HEI. I am not a big fan of after market distributors. I feel the most reliable dizzy is a factory HEI. it sounds to me like your pick up coil is going bad. you can test everything on a HEI except the ignition module. so start testing. highdesertranger
 

kaidenshi

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Georgia
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Morgan
Truck Year
1982
Truck Model
C10
Engine Size
350
first off 1972 did not have HEI. I am not a big fan of after market distributors. I feel the most reliable dizzy is a factory HEI. it sounds to me like your pick up coil is going bad. you can test everything on a HEI except the ignition module. so start testing. highdesertranger

The engine is out of a 1972 and originally had a points distributor, but the truck is a 1982 and had a factory HEI, which was the one we kept during the engine swap. Sorry for the confusion, I thought I had said that earlier.
 

kaidenshi

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Morgan
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1982
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C10
Engine Size
350
So I ended up replacing the starter (it needed it, I think the old one was about to give up the ghost), both battery cables, and the distributor (new one is a Summit Racing "blueprinted" HEI) and it's running better than it ever has. No more dead ignition module, no more missing/stumbling at ~2500 RPM, and the idle is as smooth as I've ever heard on a rebuilt 350. I think it was the Accel distributor that was the real issue, but it definitely needed new battery cables as the old ones were starting to fray and the jacket was cracking on the positive cable.

I did all the work yesterday and have enjoyed driving the truck all day today. I didn't realize how much I missed driving it!

Thanks to everyone for your help with this issue.


Morgan
 

HotRodPC

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That's the one to solve an ignition problem. Replace the whole dizzy and be done. Many of these old trucks need it anyway. I see guys who say, I have another dizzy over here I can drop in, and the bushings are shot and the drive teeth are worn so even if it does work, it's certainly not optimal.
 

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