Marv
Junior Member
- Joined
- Sep 28, 2020
- Posts
- 25
- Reaction score
- 40
- Location
- Montana
- First Name
- Marv
- Truck Year
- 81
- Truck Model
- K10
- Engine Size
- 383 Stroker
I just bought this truck a go year from a good friend(it was his father's). It was the first vehicle I was ever taken on a "hell ride" way back in the early 90's. Long story short, always wanted it and now I have it. It has the first 383 stroker that was made in this area. I noticed something was wrong a week ago and figured it was the carb. While disassembling to make it easier to get to the far back of the motor decided to take the intake off and try a different one a friend had and get rid of most emissions nonsense at the same time. Intake completely clogged on the crossover port as well as the heads. Said screw it, popped the heads off and low and behold 7&8 are cracked. So now the plan is to also change the radiator, main wiring harness, delete the a/c box, do a 1/2 to 3/4 ton axle swap and put a lift on it. Any pointers or suggestions are more than welcome. I need to have it out of my garage by Friday which is gonna be nearly impossible working by myself. I feel better now that I've typed this out and I'm excited again. This thing is a blast to work on! And he's gonna be an absolute beast in a week.
Sent from my SM-G988U using Tapatalk
You must be registered for see images attach
Sent from my SM-G988U using Tapatalk