- Joined
- Feb 5, 2014
- Posts
- 4,293
- Reaction score
- 3,339
- Location
- Kentucky
- First Name
- David
- Truck Year
- 1986
- Truck Model
- K10/LM7 5.3/4L60e/np208/3.73/32"
- Engine Size
- 10 yrs Air Force
going through this now. With a plug ran directly from the motor to battery.....it hauls arse (about 3 seconds). On the harness, it takes about 7 (guessing) seconds to go up or down. I've got the relay upgrade installed also. Almost at a loss because the harness I built is above the quality that LMC sells. My only guess, for me anyway, would be heavier gauge wire and heavier duty relays.......the truck harness/switches are basically a signal at this point.
Thought I'd share.
Thought I'd share.