Stormhawk
Junior Member
- Joined
- Oct 4, 2024
- Posts
- 28
- Reaction score
- 43
- Location
- Scobey, Montana
- First Name
- Marshall
- Truck Year
- 1983
- Truck Model
- K20
- Engine Size
- 350
Gents,
I just did a trans service on my TH 400 and replaced the kickdown solenoid, vacuum modulator, gasket, fluid and filter.
The truck didn't have proper kick down prior to the service and still doesn't after replacing all the parts although it s
Up shifts and down shifts perfectly otherwise.
I tested the switch with a multimeter and reset it with the pedal. I also replaced the spade connector on the line leading to the switch on the solenoid
What else could I be missing?
I just did a trans service on my TH 400 and replaced the kickdown solenoid, vacuum modulator, gasket, fluid and filter.
The truck didn't have proper kick down prior to the service and still doesn't after replacing all the parts although it s
Up shifts and down shifts perfectly otherwise.
I tested the switch with a multimeter and reset it with the pedal. I also replaced the spade connector on the line leading to the switch on the solenoid
What else could I be missing?