jdogginit
Junior Member
- Joined
- Mar 10, 2023
- Posts
- 23
- Reaction score
- 35
- Location
- montana
- First Name
- Jason
- Truck Year
- 1982
- Truck Model
- k10
- Engine Size
- 350
I have an 82 k10 SWB project I picked up. 350/TH350/NP208. Supposedly ran when parked right! Got the 350 engine running. Good compression. Put it in gear and nothing. No reverse or anything. It did roll a little bit in 2low but then nothing.
Fluid level was good, I thought, now I question that because The dipstick is the wrong one so I’m going to fix that. Pulled the pan. No chunks of anything but sealant. Filter was free. Fluid was red but dirty looking. Didn’t smell burnt. Disconnected torque converter from flex plate and spinning it spit fluid out the filter hole.
this is a lockup tranny th350c. The connection on the drivers side is not connected and there’s nothing to the plug inside (as seen in pics). I’m guessing someone tried to delete the lockup? Anyways I’m at a loss.
May pull it and try to rebuild but obviously if I don’t need to that would be cool.
Any help would be appreciated.
Fluid level was good, I thought, now I question that because The dipstick is the wrong one so I’m going to fix that. Pulled the pan. No chunks of anything but sealant. Filter was free. Fluid was red but dirty looking. Didn’t smell burnt. Disconnected torque converter from flex plate and spinning it spit fluid out the filter hole.
this is a lockup tranny th350c. The connection on the drivers side is not connected and there’s nothing to the plug inside (as seen in pics). I’m guessing someone tried to delete the lockup? Anyways I’m at a loss.
May pull it and try to rebuild but obviously if I don’t need to that would be cool.
Any help would be appreciated.