SirRobyn0
Full Access Member
- Joined
- Dec 6, 2019
- Posts
- 6,755
- Reaction score
- 11,402
- Location
- In the woods in Western Washington
- First Name
- Rob
- Truck Year
- 1984
- Truck Model
- C20
- Engine Size
- 305
I have the 700r4 and it shifts pretty sloppy and basically slides into gear lol. I used my dial back timing light and it was set at 40 initial, I revved it up from there and it went up but I wasnt too worried about how high the timing went because it didnt seem to ping and I knew i was going to fix it. All checks were done with the vacuum advance unhooked and plugged the hose from the carb. It did have a little valve or fitting on the line just before the dist but Idk what it is for yet. Anyway I moved the timing to 11 initial and revved it up to about 3k and the timing went up to about 40 so it seems good now. I only had to adjust the idle speed after that, it seems fairly responsive for a smog motor now and runs ok. I just picked up some true duals from lmc truck today for a change from the y pipe and single 2 inch, hopefully that will help out the power a little bit too.
Well you have the timing sorted out now and that's what really matters any way.
I'm still running single exhaust, I thought about going dual when I needed to do exhaust work but what prevented me is that my truck has a dump kit on the factory box and pump is mounted on the in board side of the passenger frame. I do not want to run hot exhaust right next to that, so I went to a high flow cat, larger mid pipe, I think it's 3" and a big 22" high flow low noise walker muffler with dual outlets. So I think it's a pretty free flowing exhaust system for what it is anyway.